[SEL] Another IHC LB Running
FRM8198 at aol.com
FRM8198 at aol.com
Sun Jul 3 21:20:30 PDT 2005
Hi List,
My latest project -- another IHC LB is now running correctly after I finally
figured out what was wrong with the governor control. There was an
interference between the head and the governor control rod. Before getting rid of
this interference, the engine operated at a fast RPM and its speed could not be
changed.
This engine arrived at my shop in a semi basket condition -- head
disassembled, oiling line off, piston and rod rusted, rocker arm and shaft rusted,
block caked in old oil, and the hopper full of debris. The head was in a very
poor condition. New valves were remanufactured from old valves. The head
seats had to be resurfaced. Replacement valve stem oiling felts were fabricated
from material obtained at a hobby shop. Push rods, rocker arms and shaft
were cleaned. New oil wicking was made from two pieces of string cut from my
wife's string mop. The shaft of the throttle control valve in the head was
frozen and had to be replaced. The replacement shaft was made from some ¼"
square brass tubing and 3/16" rod silver solder together. A new head gasket was
made from a piece of material left over from another uncompleted engine
project.
A replacement gasoline tank was purchased from Hit-n-Miss Enterprises. A
new ¼" copper gasoline feed line using the old check valve assembly was
fabricated. A bronze ball was used in this assembly along with new bronze strainer
screen. A new compensating valve disc was made from a fender washer. The
old compensating valve spring was also replaced. The choke shaft and spring
were replace. New home made gaskets were used during reassembly of the
compensator valve assembly and mixer.
The cylinder bore was in a very sad condition. A good honing remedied this
problem. A replacement connecting rod and piston along with a set of new
rings were installed.
A replacement crank handle spring and pin was installed in the flywheel.
The head of the crank handle pin was slightly mushroomed so that friction would
hold this pin in place. I didn't know that there was a small hole at the
bottom of pin hole which allowed the use of a small punch to drive out the pin.
I did it the hard way by drilling and tapping the old pin in order to
remove it.
In addition of a new high tension wire, the magneto only need a good
cleaning and set of new gaskets. An engine stop switch was fabricated and installed
on the magneto to stop the engine. Strangely, the old spark plug seems to
work after only being wire brushed.
There is a small oil leak in the side plate which still has to be addressed.
I would to thank everyone who very kindly replied to my inquiries and
questions, helped me understand how this engine was oiled, and provided suggestions
how to overcome various problems.
Francis Maciel
Santa Maria, CA
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